When working
with aluminum,
Ekblaw said,
“The question is,
When you weld it,
can you keep
it straight?”
FIGURE 2
Some sections with this X configuration oil canned. To eliminate this, Ekblaw removed a small section of
metal from the center section and filled the gap with a 100 percent-penetration weld.
Get even more
welding news with
“Welding Wire”
– a free monthly
e-newsletter.
To sign up, visit
www.thefabricator.com/ww
is an officialWeb site of the Fabricators
& Manufacturers Association, Intl.®
Minding the Heat
To start welding, Ekblaw tacked every
joint, evenly distributing heat around
Nereus. He then locked Nereus to the fixturing table and began welding, again evenly
distributing the heat by shifting between
the port and starboard sides and making
shorter welds.
Unlike welders who leave a machine’s
balance control set in one spot, Ekblaw uses
the AC balance control to adjust the ratio of
cleaning action (duration of the electrode-positive half-cycle) to penetration (duration
of the electrode-negative half-cycle, when
the heat flows from the tungsten into the
workpiece).
“I really like Miller square-wave machines
because of their balance control,” he said. “I
make constant adjustments. As the heat
builds up, I turn down the penetration. If I
see the weld puddle is a little cold, I turn up
the heat.”
Ekblaw welded Nereus only in the flat,
horizontal, and vertical-up positions, moving
Nereus’ frame as necessary.
“I think vertical-up helps ensure good
fusion, and I can see the joint better. With
vertical-down, I would be worried about
the puddle rolling over the top of the joint
and causing cold lap,” said Ekblaw.
Despite Ekblaw’s best efforts, distortion
occurred. He explained, “The center pipe
shrunk 3⁄ 4 inch. I could see from the centerline that my layout was perfect, but welding caused the pipe to shrink 1⁄ 2 inch, and
heat treating caused it to shrink another 1⁄ 4
inch. Fortunately, the distance between the
two pods doesn’t affect the design. Our primary goal was keeping the pods parallel,
which we achieved.”
Welding heat also created an old-fashioned oil can problem (see Figure 2).
The smaller sections on the bottom of the
pods designed with an X configuration had
insufficient mass to dissipate the heat of
welding. They subsequently popped out of
plane.
“On the sections that oil canned, I cut
out a small piece of the center section and
rewelded the halves. As the weld cooled, it
shrunk the section and put the part back
into true.”
Overall, Ekblaw said it took him 80 to
100 hours to weld the pipe main cross
member, the two outside frames, and the
manipulator arm sled, using about 35 lbs.
of filler rod in the process. ■
Woods Hole Oceanographic Institution, 266 Woods
Hole Road, Woods Hole, MA 02543, 508-457-
2000, information@whoi.edu, www.whoi.edu
Miller Electric Mfg. Co., 1635 W. Spencer St.,
P.O. Box 1079, Appleton, WI 54912, 920-735-
4141, www.millerwelds.com
14 PRACTICAL WELDING TODAY
May/June 2009